2023年6月,有飞机因发动机进气道防冰活门故障,在更换完成右发防冰活门,恢复M项后,出现右发高压级活门维护信息,故障代码为36-11021,从监控页面看,高压级活门失效在关位,并按MEL锁高压级关位放行,航后解除高压级活门人工锁定后,执行AMM36-00-00-730-801.Pneumatic Engine On – System Test带引气的系统测试后正常。
(a)System was in EAI HOLD mode (EAI was ON and aircraft was in the icing envelope below 22500 ft (6858 m) and not descending) and PI pressure was less than 45 psig (310 kPa) while HPSOV was commanded in pneumatic mode (Torque Motto Command less than 2 mA).
(b)PI pressure reading was VALID and PI overpressure was less than 170 psig (1172 kPa).
(c)PI pressure reading was VALID and HPSOV was commanded closed (Torque motor current more than 110 mA) and PI Pressure was not at least 20 psig (138 kPa) lower than the PS3 Pressure while PS3 pressure was above 45 psig (310 kPa).
(d)HPSOV was commanded open (Torque motor loopback current was less than 2 mA) and PI pressure below 16 psig (110 kPa) when engine was running engine supplied HP port pressure was above 25 psig (172 kPa) and PM was either valid and under 13 psig (90 kPa) or not valid.
2019年6月6日,海口白班检查双发HPSOV锈蚀,双发引气系统测试有状态信息 BLEED HPSOV L和BLEED HPSOV R信息,左发代码:36-11020 ENGINE-1 HPSOV IS NOT IN COMMANDED POSITION Detected by: INTEGRATED AIR SYSTEMS CONTROLLER (IASC)-LEFT,右发代码:36-11021 ENGINE-2 HPSOV IS NOT IN COMMANDED POSITION Detected by: INTEGRATED AIR SYSTEMS CONTROLLER (IASC)-RIGHT