MAX飞机布罩大小刚好能罩住进气道,如果外侧上部的钩子挂的太低,就会出现进气道下部无法完全罩住,长期还容易造成布罩损坏,需维护中注意。

MAX飞机布罩大小刚好能罩住进气道,如果外侧上部的钩子挂的太低,就会出现进气道下部无法完全罩住,长期还容易造成布罩损坏,需维护中注意。
LEAP-1B 发动机的燃油喷嘴,也有积碳(结焦) 的安全隐患,尽管此问题可通过加装 CFM即将发布的 RBS 系统后得到解决,但当前的过渡阶段仍然面临定期更换全套(或部分)燃油喷嘴问题。此拆培训材料用于拆装步骤和安全方面的提醒。
2023年5月,有MAX飞机反应MAINT灯亮。
状态信息1为SPOILER CONTROL CHANNEL ,相应维护信息为27-01330 GROUND SPOILER OUTPUT DRIVER SIGNAL IS OUT OF RANGE Detected by: SPOILER CONTROL ELECTRONICS (SCE);
状态信息2为GROUND SPOILER CONTROL,相应维护信息为27-01220 GROUND SPOILER CONTROL MODULE IS NOT IN COMMANDED POSITION Detected by: SPOILER CONTROL ELECTRONICS (SCE)。
复位P18-1 B4 和P6-1 A16跳开关故障依旧,整机断电后重新上电,故障依旧,27 – Spoiler Control, SYSTEM TEST, Ground Spoilers测试时发现地面扰流板升不起来,27 – Spoiler Control, OPERATIONAL TEST, SCE Test测试通过。
27-01330 GROUND SPOILER OUTPUT DRIVER SIGNAL IS OUT OF RANGEDetected by: SPOILER CONTROL ELECTRONICS (SCE)的可能性故障部件为:
(a)The ground spoiler control module, M2988.
(b)The ground spoiler control relay, R1169.
(c)The spoiler control electronics, M2940
(d)The problem with the wiring.
27-01220 GROUND SPOILER CONTROL MODULE IS NOT IN COMMANDED POSITION Detected by: SPOILER CONTROL ELECTRONICS (SCE)的可能性故障部件为:
(a)The ground spoiler control relay, R1169.
(b)The spoiler control electronics, M2940
(c)The ground spoiler control module, M2988.
(d)The problem with the wiring.
从故障信息看,SCE取的是GSCM的预位和控制电磁线圈的电流值,用于监控是否在可控范围。当不在范围时,就给出相关警告。从排故结果看,是R1169故障导致的。符合IFIM中关于27-01220的故障可能排序。SCE自检测试能通过,也表明SCE是没有问题的。关于GSCM内部液路作动原理课参看另外一篇关于扰流板无法收回的说明。
截止2023年6月,波音全球的统计数据如下
RECOMMENDATION: 27-02790 SPOILER FAULT OUTPUT DRIVER SIGNAL IS OUT OF RANGE: Operators have reported SPOILER CONTROL CHANNEL status messages. Boeing finds these messages may occur during power up, often with maintenance message 27-02790. To minimize the chance of dispatch delay, Boeing recommends to perform the following FIM based maintenance checks for occurrence of SPOILER CONTROL CHANNEL status message with MMsg 27-02790 (SPOILER FAULT OUTPUT DRIVER SIGNAL IS OUT OF RANGE): – Use the OMF to perform the ground test 27 – Spoiler Control OPERATIONAL TEST, SCE Test. -Refer to AMM Task 27-61-45-730-801 – Spoiler Control Electronics Self – Test. -Note that the SCE ground test requires the Master Dim and Test (MD&T) be in the bright (BRT) position. -Confirm the MMsg 27-02790 is cleared by the Ops Test. -If cleared, the system is OK for dispatch. -If the fault is still active, use FIM Task 27-61-00-810-922 to troubleshoot and diagnose the issue. MEL dispatch relief is available for SPOILER CONTROL CHANNEL. MEL 27-61-01-01 should be reviewed for applicability. |
MITIGATION: 27-02790 SPOILER FAULT OUTPUT DRIVER SIGNAL IS OUT OF RANGE: Boeing and the SCE supplier (BAE) are investigating the root cause of this message and assessing the appropriate Spoiler Control Electronics software change(s) to appropriately address these faults. |
2023年5月有飞机在关车后,出现“ENG 1 0IL DEBRIS SENSOR”状态信息,含义如下:
The EEC will set this message when the oil debris monitoring system (DMS) sensor is failed for 5 seconds.(a)This fault is only detected and annunciated by channel B.
代码为71-09001 “ONBOARD MAINTENANCE FUNCTION HAS NO INPUT FROM ENGINE-1 EEC”,737MAX-FTD-71-22002对该信息做过说明,如果将EEC置于TEST模式,则可以清除故障。同时波音建议如果发现MAINT灯亮,波音建议运营人
不要将MAINT灯与维护信息71-09001与/71-09011联系到一起,并采取进一步的排故来寻找MAINT灯亮的来源。
实际操作中,检查DMS都是0,给EEC通电后,维护信息消失。
状态信息,也可以参考MEL保留放行。
备注:该信息,AHM未有记录。由于改信息发生在关车后,同时结合71-09001维护信息,磁堵状态信息的出现,我们的理解是EEC断电时,使用EEC作为激励供电的断电次序引起的。可以考虑第一次不做排故当再次出现磁堵的信息时,对传EEC,和更换传感器。
后续:隔离位传感器故障。但排故过程较为曲折,因为第一次更换的传感器为故障件,后续又更换了EEC,量线等工作。